Time to get my cnc machine up and running again!!!

time to revisit this.

As my pc died over Christmas I have been putting this off for a while but now want to make some bits and the CNC will be perfect for this so I am going to get the machine working. and do some more modifications to it on the route. this is a 3040T Chinese milling machine.

I am also going to try CNC carving and milling with fusion360 as prior I have used other packages but seeing as fusion 360 is my go-to for design. as I learned on AutoCAD it shares a lot of similarities. more on this later.

The Story so far

This is so you don’t need to go back through the site. I brought this machine thinking CNC was easy as 3d printing and laser cutting it’s not. had the machine collecting dust for a year. during lockdown made an enclosure modified the machine to add some custom made end-stops and got rewired it and had a light bulb moment. then made a custom wast board with threaded inserts.

So as I wait on components from china for the cave monster time to clean out the enclosure and add make some bits to make my china CNC machine great and teach myself some more about CNC.

the spoil board is where I got to last time before the crash. and was working on a custom dust shoe. then other projects took over so I’m now going to start to make more stuff on my machine. So this I blog of my progress. see the photo montage below.

Time to clean my machine

As the machine has been sitting for a year since I last switched it on.

Before I get started getting a feeling I am going to need to clean the cooler water for the CNC machine, Ok not terrible but needed a cleand as organic material in the bucket. out with the old and time to clean the bucket fill it with some a 50/50 mix so 5L anti-freeze and 5L of deionised water as then bucket should keep it nice and clean going forward. now to pump it through the system see the pink in pipes and check for leaks, no leaks.

Now I have a clean machine I now to set it all back up. so over to the pc well remote link to the pc as it’s cold outside. so installed a remote desktop on the cave computer and have the machine running as the control box is on.

The Setup

Now to find my note as need to revisit them and get all the settings plummed back in.

Have installed mach3 need to install a plugin for the control board and MPG luckily have saved all this all in my dropbox so just drag and drop it all into my mach3 folder.

next up remembering pin set up so port 3 pin 1 = estop pin 2 = home switch pin 3 = limit switch and pin 4 = probe plate. so into inputs check there all right and enabled they are.

following the Chinglish guide, I go through the motor tuning and select all the right bits.

Config menu ports/pins

make sure all motor axis are selected

Next select input signals copy below

as i have added home and limit swtiches this is off wha the manual said now scroll down and enable estop and prob.
all done

Now over to output signals tab.

now to click ok

Motor tuning for x y x follow below

now for A and splindle

now spindle

dont for get to hit save Axis settings after each change.

now one thing i forgot to set limits and homing that will mean your homing in revirse so on x and y dont forget to home Negtive only on x and y and your golden i have also set up the soft limits to prevent from crashing.

now to home the machine hmm it all z homes right x and y

adding edge finding and z zeroing tools scripts I highly recommend checking out


The legend that is Charlie Sarsfield followed his instructions on adding limit and home switches and his tool zeroing and edge finding scripts and install them

and now to make sure the machine spins and does what it’s meant to all works fine will be adding a new calibration plate so will test the scripts work like a charm

So the machine is back to working but me being me time to modify it some more.

Upgrading dust extraction system

before I start running some projects I am going to revisit the dust extraction as it’s okay just not brilliant lots of leeks for dust. so I’m going to make this modular and dust-tight hopefully I have added some fins to my dust shoe so it should suck all the dust-up am also adding parts so that vacuum tubing that will go through a flang that I can plug my shop vacuum in and out of. so over to fusion 360 to model the flange.

outer flange

now to test fit that before I make the inner flange. well it sorts of works i forgot to attach the inner tube so is floating so now making 2 outer tubes one so made them box the 35,2mm inner and then made so it will fit over the centre tube then enlarged it out to 36.5 mm with a 45mm outer

as for the tube end, I have made an inner opening end for 39.5mm and the flange end made it 35.2mm have then glued them to the flange. and screwed it to the enclosure. I forgot to take pictures doh here it is partly assembled with a vacuum hose attached from the vacuum end.

Have 3d printed a nozzle for the 40mm vacuum tube that I have a 5m length that i brought previously so I could extend the hose for the shop vacuum. I found a design some time ago and had test fitted it so I have cut down some vacuum hoses for the internals of the enclosure now going to print some clips to secure the hose internally to the roof of the enclosure.

all plummed in have ordered a new dust shoe from that has arrived fits well got to make adapter tube up infusion nothing flashy inlet side is 38.5mm and output of 36mm

quick sketch

2hrs later and it fits like a glove just need to trim down the hose lenth and install clamp

as now can plug the shop vac in and out. I might upgrade that too as is not too powerful think that will be next month’s shop if I feel it needs it.


First up I needed clamping arms as I had a few issues with the tape method that everyone raves about. i might revisit this

so found some CNC clamps that I saw teaching tech use on a video so going to give them ago I will also test out some style ones as well as I need different ways of clamping down materials.

So new untested eSun PETG filament loaded into neon orange and away we go will check seems to be laying down fine layer 5 and only a little mess on the bed will check back later.

work fine now to re set up the machine

have now printed 3 diffrent styles will be testing them all out once I have the machine up and running. as we have some nice weather coming over the next few weeks willl get some diffrent materials as well.

3 different clamp types

I will be testing them all out I have a feeling the big one in the middle is too big for my hobby CNC machine.

have also designed my own one as well will do seprate post on that as this is already gone from being a quick post to entertaing me to another

Zeroing tool upgrade

Next up going to change my zeroing tool for a new one I have purchased off eBay.

as I was clever and used the power connector just need to unplug the old one and swap the wiring over now. All done and the magnet works well no hassle of crocodile clips well worth the £30

now back to the automated edge finder and tool z hight scrips now I know the XY thickness is 10mm and the z is thickness is 12mm so need to change the variables as shown below.

time to test the system

test complete have moved the plate off material and hit go to zero not bad going it a little off I didn’t set the tool diameter so that might be the reason it’s away from the corner.

Setting up Chinese CNC with fusion 360

Now I could do this using a different method as having used other CNC design software in the past and still have access to it but me being me decided I would go another route as keen to learn more about fusion as it is more than just 3d modelling tool.

So time to put some scrap wood in and see how we go, going to start with something simple as I am going to use my go-to program for design to try the manufacturing side of the program that I have no experience with so going to make a pocket in some wood with a simple part to see how it works.

as with anything design related i need to take some measurements so i am going to start by measuring my scrap of pine in the machine, I make it 200mm x 200 mm x 12mm then made a note of this so when it gets to it the program will know how big the piece is. i am going to machine is.

Next, i will need to make a list of tools as all the sample tools are developed for big milling machines with quick-change collets one day when I have a big workshop I will get a bigger machine. but for the time being, mine is only 3040 well actually it’s less than that more like a 3727.

time to gather some data for tools so I have ordered a set of six tools from china and with that i have the following data. so going to add them to the system along with some end mills and facing tools that I have in my collection.

incoming bits from china

I have also found prior information on some other bits I ordered in the past so been collecting them in a file to add as well.

will need to add these as well

The tool adding can be found in utilities under tool management

Click library then click the plus icon you will be greeted with a tool selection screen

you will be greeted with a tool selection screen screen

so in this case will be adding a 6mm end mill so I select the end mill.

Time to give the tool some description vendor name as I don’t have a link or id won’t add them.

tool i am adding

No to add cutter detail so I have this information on the tool

all the information added

I have copied speeds from another package as the default 5000 speed on the tool was mega slow. so have now upped it to 16000 and have calculated a minim feed rate 17.882 meters per min now running it 650 feed rate as 18 was way slow for wood.

now hit ok as don’t have a holder template for the depth of tool 0 as I don’t think it’s necessary as will zero tool after each tool changes this is more for an auto-loading tool machine perspective.

tool set up complete

So infusion I have made this test part nothing special just make some pockets and will do more if it works this is a stage of learning so let’s see how it goes.

test part is not needed for anything just a quick sketch to see if it works

Now to switch from design to manufacturing add the tools then let’s see what they do.

manufacturing mode

Now for the set up this did seem a little daunting in the beginning think I have figured it all out I am going to only use one tool as this is experimental.

Click the setup button I am first going to move the origin from the centre to the front of the design is the same as the stock size it’s easy just click the dot on the front. as show below

Origen now front of the pice.

now the stock tab I have changed the stock to be relative to the box with no offset.

The dimensions from earlier 200 x 200 x 12 and the stock match perfectly

Next to the program number and comment.

just added a comment and then press ok

now we have this set up I am programming in a 6mm end mill so adding to the tool library.

so have programmed this six mm end mill in as the quickest one to add

first up going to perform this in 2 processes first am going to be pocketing the selected areas in the design then I will boar out the corner holes.

so to start going to the 2d pocket will then set the tool as my 6mm endmill. I will then select the 5 areas that I need to pocket out. click ok next under the 2d tool panel i selected the boar function with a 6mm tool selected each hole all 4 of them. selected ok.

I have run the simulation and it all looks like a good time to test it.

time to test it.

Time to post-process it then load it to the machine. and zero tools find the edges and we should be good to go.

The file generated not sure if mach3 accepts that but let’s have a look

Ok, the .tap isn’t recognised as a file in mach3 but I duplicated the file and changed the extension to .gcode will now load this into mach3 and see what it spits out.

loaded as you can see thinks the part is top left corner need to zero the tool to material height and find the edges using the zeroing tool and edge finder.

right zeroed the tool correctly and fount the edges got to love the auto edge and z finder. as you can see the image has been generated to fit the stock

right that’s worked will run the test programme and see what happens to wish me luck. Ok, that failed as it went in the wrong direction. I think the Origen is reversed going to change that in Fusion 360 then try again.

ok, I am a tit missed out on something from setting up in the homing limits in mach3 doh so I needed to tick 2 boxes. now homes correctly. as I am here also going to set up some soft limits so this all works right.

Away we go slow but steady think I need to mess with the speed and feed as it’s in and going down yay and the clamping just failed.

As I have caught covid again in bed writing this so have had some time to reflect on the failure of the first run. back into fusion 360

go tool management and time to set some parameters so Spindel speed upping to 16000 and 650 meters per min feed rate I have also added multiple depths so it will now not go down 18 mm and try cutting out so now have set it to 5mm per pass switched to 2D adptive clearing.

let’s try running this test program recalculated with new clamps fingers crossed, going to use the same blank as woods not cheap and being pine won’t kill me on the dust.

first, to zero all parameters so out with the new zero tools and find the edges going to jog the too over the zero probes I have a magnet connected to the tool then on mach3 hit tool zero. the probe will go down and touch the plate touch and retract then go to jog x side of the tool and go to offset screen and hit auto x will move to the x-axis side of the tool and retract repeat on Y size using auto Y same will happen tool will move to the tool and retract system all zeroed now to remove tool and magnet off a bit. hit zero and the tool will be sitting just above the bottom left front.

Now to start the program away we go.

working but feed rates way off so going to update .

so back in to fusion as my gcoding days are long time ago so i am letting the program do the legwork. as you can see scraps had some battle wonunds not to self dont go to zero all when tool is down in the wood hoping it will be machined over have stopped the job. time to restart it. as the rate it was running would have taken a long time machine. now upped feeds from 18 to 650 mm/min so will now run the final 4 pocket first one turned out well.

so have removed one pocket out of the design i think will run some other processes on this modle as i go but will attach the dust shoe as well as could feel dust in the air. but think i am going to leave that for another post as this has dragged on all week.

Now that I have figured out the basics I want to try running some projects carving from an STL file. making a 2d PCB and then using a bit to drill make the holes and engraving tools to make the tracks on single and double-sided copper PCB board, make some complex parts out of aluminium and more. these will be broken into different learning posts as don’t want to bog down this blog so will be another post as I learn more about both the software and machine.

Parts Incoming just had a bumper instalment of bits. so will be a post about this soon as want to make this a quick to set up stable.

How to remix a stl in fusion 360

you will need a licence for fusion 360 I have a free hobby licence that is limited but till i get time to learn the cam side of the program it’s free to me unless Autodesk feels kind and wants to give me a licence. not that they will read this anyhow.

open up fusion 360

the file I am going to remix is this spray can holder.

the file can be found here

Now to remix it or in this case, I am going to create 2 bars for aligning it on the wall by using its original parts as a template. over to fusion

then go to insert drop-down insert mesh

you then can position it how you want i this case will keep it as it is so select ok,

now press s on your keyboard then type mesh you will select convert mesh.

Now select the stl

then hit ok on defaults as all other options only in paid verison.

sketch will now look like this

at this point you can simplify the sketch and make it fewer polygons by selecting segments and removing them hitting delete as shown below

So why do this well on flat surfaces makes it easier to select planes.

go to the sheet metal tab select Create Sketch, you are now going to select face to edit.

select highlighted plane and click you will now see it like below.

I am going to start off making a bar so i am going to hit L on the keyboard and will give me a line command.

as I am using snap to have determined the endpoint where I want to start the line click mouse to start the line

I next go to the bottom right corner of where I want the box i am making to be this will give me a guideline.

like below can now draw the 2 lines needed

close the shape

Now hit enter.

so that is literally the only bit i need for my idea but actually going to 2 as I want the top and bottom lugs to make int to alignment bars. so going to repeat this process and then we will continue.

I am now going to remove the original part from the system as i have the 2 elements i require for the alignment bars as will be easier than removing all the material I don’t need.

then hit del and sketch will remain

now to extrude it on both parts 100mm as think it’s a good size so hit E on the keyboard when selected object

hit enter and repeat on the bottom section of the file now change view please not i have moved them together for illistations.

Now to make the parts you now want to go to utilities tab select make

select the parts and in chose options as 2 body will need to do this twice.

this next part is as I have set my Prusa slicer to open when I make them so at this point you could save them as stl

now the part is in my slicer i am going to set it up for print by changing position before i save it out as an stl.

first to make it flat to the bed i will use the place on face tool F for a quick keyboard cheat

will select the bottom face

part ready to print in this case going to save it as a stl.

click the part then right-click and select Export as STL

save and parts done. then added them to one file ready to print will show more detailed remixes soon

then its over to the printer via octoprint in my case and away it goes as i have doubled up the parts as to racks going on the wall will take 2hrs to print.

parts all done ready for a test fit.

can find my files here do love a quick 1 day project parts are in to finish off the cr-10 so that should be up soon.

CR-10 Upgrades part 6

this has been a bigger build than I first expected around 100 hrs of printing a lot of remixing was involved so some things worked some things I have had to print again and again till correct. think they are all correct now as they fit for me.

As will any project files they are a work in progress. still need to reprint final fixes to test but the current design work with some drilling or being an angel so no rush for me. i would say there are a good few days of printing involved with this project. but well worth it.

So what this part covers:

  • All in one Cr-10 Remixed for Dual Y-Axis linear rails kit
  • UPS 12v big tree tech
  • Filament runout sensor big tree tech
  • Modifing TFT screen firmware.
  • Dragon Hotend and issue correction
  • BISQU Flexplate

All in one Cr-10 Remixed for Dual Y-Axis linear rails kit

This is a remix of this design by Cornely_Cool  can find the original design here. you will need these files for some of the builds my remix replaces the front-rear panels front left panel and several of the base plate files. this is a work in progress it works for me as of me writing this blog post.

The link to the files can be found here.

So why am I doing this the original printed mod I built-in part 3 or 4 doesn’t work with the upgraded linear rails so It doesn’t fit so going to make something using an existing design with a remixed twist as its not 100 % right for me due to the dual linear rails and the design wasn’t using SSR and some other bits. First up going to salvage parts and order up some metal work going to raise the machine 60mm and have another 70 hrs of printing ahead of me first up parts. needed some aluminium 2020 and 2040 some connectors to hold it all together some corner plates and some new rubber feet as I disposed of my original feet from my cr10 also have hight clearance is an issue with a shed roof. might still need to lower racking. have also ordered a small 5v 3amp PSU to internally power the pi that’s running the printer. as this is a custom build have also ordered some aviation plugs to tidy up the wiring and install better-suited wiring. I will have a sonsoff switch as master power on and off and use relays to turn on and off power and lights for web camera. I will publish a full shopping list. end of the post when I have calculated what I used and what you will need. will add build of material

Time to start the remix so starting with the base panels going to remix the Mosfet panel as don’t use one as running a silicon heat bed. so will house SSR relay, a 2 channel 5v relay for lights and printer and UPS board if and when it all shows up.

this is done using the panel as a reference and using PCB footprint diagrams have added a 6mm standoff for each part.

will house SSR UPS and 2 channel 5v relay it a work in progress relay fits just only screws fit

Next up I am going to remix the raspberry pi and pi PSU plate as I am going to use a hard-wired PSU 5v 3A so will need to make some mount holes for the PSU but first going to test its powerful enough. as I don’t have a reference diagram going to photograph the underside of the PSU and measure it using it as a reference image. will then trace holes for mount. won’t print it till I have tested PSU. have made some air vents and bars so i can make holes to mount it when it’s done.

the PSU holes are off as on the wrong side but will drill and bolt PSU in place. The final file changed but might be off.

The final modification is to the mainboard fixing plate so used the existing plate as a reference for size then added footprint overlay to trace holes for mounts.

the final hurdle was going to print the massive PSU plate on the cave monster cr-10 but due to wiring snagging I cannot print on it so into Prusa slicer have cut it in 2 will print half and half on both the Prusa so I can do it in half the time will line up and glue the halves together.

Now that I have remixed all required base plates now I am going to centre the middle post I have remixed the font panels to be blank as due to the dual linear kit I cannot fit a front-mounted screen. so going to remake the panels to smaller and more central with a 5mm notch to allow for fixing plates.

Gone for a central notch 5mm deep changed it again since this maid it longer.

Next, up is the power plug panel got to notch this and move the power connector as it’s right in the way of the plate.

slotted for brackets with 5 mm and move power connector by 20mm to the right changed it again as just on the borderline.
slotted by 5mm ready to print.
The last plate finishes just base plated to finalise. just had to add a hole for cables for the screen

The last panel was modified for screen cables for mounting to the frame.

Time to start printing I am going to run it all in PETG. time for some overnight parts I am going to set my Prusa’s going shame I haven’t reinstalled Octofarm to run this but will do on the next build as will be running 3 printers in it. About 4 days in now all printed apart from pi and PSU mount that’s currently running and some fixing brackets. time to build the base has been tweaked the construction of the metalwork with some extra brackets to make sure this going to the stable with the printer on top of it.

last part on the prusa printing then to assemble it all.

Oh wait fan director last 8hr print that’s overnight parts for as I am already deep in assembly.

last print of base builds overnight parts.

Time to build it.

Time to put it all together for the final time hopefully and I can then put a pin on this machine.

first up assembled outer frame with base runners and corner plates with the feet i have brought. will bolt down the centre rail once I have centred it on the base plates.

now I have a squared base I will add the uprights and bolt them down with the L brackets i have sanded the tabs on the printed walls so starting from 2040 I placed the first part I then added a bit of 2020 in the middle and continued on till all the walls was installed then using 2040 plates i bolted the base to the 2020 uprights. I will add another bracket on top of this to secure the printer to the base.

now on to the base panels, I will place them loose before I add the fixing clips in place.

all my components line up perfectly well almost but still bolts down sold just need to adjust the centres slightly as the footprint diagram I found is wrong on the relay. I am getting better with each project build. now everything is in place have added the clips have bolted down all the components apart from PSU as need to modify it for the upgraded fan.

fitted new PSU base plate but holes are off, needs to modify

Final version the pi & PSU plate is done holes are wrong but I just drilled new ones and screwed it down with some 6mm M3 bolts I will start wiring up tonight.

actually going to need cable management. so time to fire up the Prusa 1 more time for a plate of connectors.

the last print for the base.

The wiring

First up will run the mains wiring from the 3 pin kettle connector to the Sonoff switch then across the on/off switch for the pi PSU and the main printer PSU. now I have the main power in.

Main power all in forgotten my wifi password so I cannot test the Sonoff all fit perfectly.

Next, I will run negative connections for the 2 channel relay and link the relay to the pi so I can control it via Octoprint. I will then run the positive to the PSU and lights circuit for the web camera. next up are the jumpers from relay to the raspberry pi going to use 5v ground gpio 23 and 24 pins I am also going to use 3.3v and pin 9 ground and pin 14 for a temperature sensor inside the enclosure so I can adjust the fan if it gets too hot inside.

Ok, my worries about the mini PSU and voltage is fine there is no under-voltage which is great as sometimes things are not what they are advertised as.

time to pull out the wiring diagram for the mainboard.

list all connectors as you can see negative and positives are needed on end-stops and thermostats if not get kill alarm so on the end-stops and thermostats square is= to ground.

end stops and motor connecotrs are wired board side got to do some soldering but will cover that later as need to make some new wires for the heat bed and y-axis.

I am actually going to modify one of the front panels to house a Micro sd card reader and a fan speed controller PCB so back into fusion 360 going to add foot block and add 2 3mm holes to mount the front 2 PCB holes as then in the main plate I will add an 8mm hole for the potentiometer. then over the other side of the panel, I am going to cut a hole for the sd card reader to squeeze into I will then fix it with hot glue. as the original design used a USB switch to allow for firmware update the skr board only allows for MicroSD upgrade so as the board is going to be embedded this will allow for firmware upgrades in the future.. this will be a 4 hr print I think. as I test fitted the 2 halves I needed to reprint this anyway as it’s off by 10mm so now will fit perfectly under the front plate support

So out with the callipers, I go to make everything will fit and is sized correctly. time to modify the sketch.

will do an overnight prototype print. well, morning has come and yes everything fits fine just need to screw the PCB down and hot glue the sd card extension in place and we are a bit of sanding for the tabs and should be good to fit. note to self make sure you sand the tabs another 3 hrs print and will defently resand the front panel as snapped a tab these things happen when prototyping but its starting to take shape.

whilst I’m at it going to add 10mm space on the rear power panel as it was very tight prefer there is some wiggle space more airflow as well going print it on ultraviolet tonight back on with the assembly tomorrow.

redesigned as was too tight on the centre spacers.

All panels are now fitted going to cut myself an aviation plug holder jig. so out with a sheet of acrylic time to cut and bolt together.

So over to light burn a sheet of acrylic in the machine let make this design I got off Thingiverse https://www.thingiverse.com/thing:4201220. I have relayed it out slightly different as I want to fit on a sheet of 300×400. if someone wants it will share it.

as I want a good connection going to start with the 4 pins i have given up on the six-pin as NEMA wiring is too fragile.

ready to cut.

Not everything you find on Thingiverse is right so had to modify the file slightly to get it to work but now a more compact jig. as the dfx is segmented and didn’t cut right in light burn fixed now and modified the base as was too big for smaller workspace ready to solder tonight. got 1 socket to solder

assembled ready to make my new connectors

Nice and neet now for the heat bed connector need a new connection as the board is about 20cm further than it was originally also my bad soldering means it intermittently doesn’t work. so time for a fresh connector.

time to solder up a new heat bed connector with longer wires so I can wire direct to PSU and solid-state. out with my soldering iron I know the following

Pin 1 = Thermostat Positive if wired wrong alarm will sound on SKR board

Pin 2 = Thermostat Negative if wired wrong alarm will sound on SKR board.

Pin 3 = Heated Bed as 220vac voltage don’t matter which goes to witch

Pin 4 = Heated Bed as 220vac voltage don’t matter which goes to witch

have put continuity meter across the pin and end of the cable and they all check fine

now to wire it all up and we should be good to test.

all ready just need to shorten the neo pixel cable as made it way too long. going to use the bit I chopped the neo pixel wire I will use for the filament run-out sensor cable. Then it’s time to finesse the cable management.

The next issue the fan direction vent is hitting the y axis so going to make my own custom offering so going to find the footprint of 120mm fans going to make it easier to fit low profile fan shrowd. should have space as gone for 35mm high to 19mm high

So should have good clearance space. 6hr print will run tonight need to swap filament as running low on Neon orange.

Done just need to see if it fits

The wiring list is getting shorter just time consuming getting there.

end stop and motors temperature sensors and relay wiring left before I’m done.

Time to link the raspberry pi to the relay using 5v ground and pins gpio pins 23 and 24.

Temperature sensor installs time so using 3.3v ground and Gpio pin 14 for the probe have added the Dupont connectors to go over the gpio pins going to have to do some changes via rasp-config to let the system know pin 14 is sensor pin. but will check if this is needed or not as it is an old guide I read. I will also need to add a plugin so it will display the internal temperature of the enclosure so I can monitor and adjust the fan speed accordingly.

going to have to change the sensor type as this type I have installed does not have a pull-up resistor on it so just ordered another type off eBay so will swap it out.

Finally, The wiring is now all complete just need to test everything works.

finished all internal wires oh wait missed the lighting circuit Relay.

The camera light relay I have pre-made a cable from the 12v supply the positive will go to the power connector negative will go via the relay so I can switch camera lights on and off when a print starts and ends. have had a change in the design as I’m not using USB switch going to wire power connector to where the switch was going an install an A to A USB panel mount so I can connect the camera to pi externally power will be via the relay so I can turn halo on and off if required, should have parts Monday. as I wired the power socket tonight I had a thought about the USB connection wouldn’t work. back over to fusion 360

power for light rig is in.

Designed the first version it’s printing now but it’s not going to work as needs relief for the screws so have remixed it further and come up with this going to print it so have both options but think this is the winner.

v2 think this is the winner

As you can see from original to remix v1 and final v2 these are the things you have to take into account when remixing a project.

orignial version 1 and 2

In fact, I am going to redesign it again as the cable layout is different so back into fusion I go doing a scrapy print to see if it works but this should be the final design have made a few changes including screw head relife and it fits perfectly added to the remix pack

version 3 with cut out for plug that turned up

this project is pushing my design skill and I love it.

the finished item I do love playing around in 3D print.

Time to fit it all into the machine.

Right, I am on the home straight I need to make some form of protection for the printer’s innards.

going to cut some black acrylic insert them in the middle of 2020 extrusion as dust covers.

so been thinking about how to do this without having to remove the front of the printer going to do some testing. I am going to cut some test bits 20 x 74 mm at a start to see if I can insert it then centre and add a fixing clip to hold it in place I will then make will also design a middle clip that can be removed to gain access. well,

that’s the idea, time to make some test bits. so over to light burn and as I have some offcut left from the jig build going to cut some strips to see what can be inserted,

time to cut some interest to test have labelled them for ease of use

So looking front on Left = 77 middle = 146 right = 75 now to make 2 x 200 long size X plates for each area will then 3D print the customizable design for centre plates then to design some clips that will be after I have the covers fitted.

I have decided to make it a 3d printable version obviously they will be subject to where your cross braces are. but you can customise them in the slicer. i am going to print my covers so they match the base as I could cheat but I want this to be a mostly printable design. also, put a clip together

the first plate is printing

here is the centre plate design will be making left 70mm, 138mm and right 68mm. the centre area 72mm across. total area 100mm

Clip design I have put these in to hold the panels in 3 per panel so 24 in total. currently printing a sheet.

final plates are printing on the printers should have all the dust covers done tonight then I am ready to assemble the 2 parts have hit one minor snag as the end stop bar is skimming the middle plate need to take a few mm off it to get it to work right will think about how I do this might just be a shorter screw and a 10mm off the tube with a hacksaw. No, I own a 3d printer. so now printing a shorter 11mm x 20mm tube and have a shorter screw to fix the issue.

only issue is the centre plate as the end stop bar is clipping it.

All fixed worked like a charm now does not rub on plates and makes contact with the endstop. all plates fitted made a cut out for dust cover so waring was more neat.

Dry fit works well.

dust covers all fitted and wiring from neo pixel hidden also hidden the filament sensor wiring if there’s any interest will publish all the other bits I found on Thingiverse that used to help with the project.

Yay parts from china

Just as I was about to put a pin in this build and post the post I have now received parts from aliexpress so back on to some more upgrades. lol so this will be tomorrow as one PCB to fit and wire and one sensor to attach. and a Flexi plate to stick and fit.

So a new day has dawn going to try wrapping this up today bar printing or tuning.

UPS big tree tech

This should be easy to install one 3 pin plug to the mainboard from the ups and 12v supply just got to figure out where to place the board in the enclosure I think I am going to make some holes and add some standoffs as I did with the 2 channel relay. need to look into firmware changes for its use will cover this at the end of this post.

My fingers are crossed my calculation for the footprint of the board is correct and this just pops in with some m3 screws. Well, I’m too good fits perfectly just got to finish wiring it up.

Make sure that the + & – are wired correctly as will destroy the PCB if wrong they are labelled on the bottom of the PCB then links them to the power input on the mainboard like shown below.

then insert the 3 pin connector and connect to pwr-det on the mainboard and then back to ups PCB and it’s all installed hardware-wise.

Now for firmware changes

There are 2 files you will need to change first is in the feature folder look for powerloss.h

I have changed debut and saved each cmd this will save the last state on the printer if there is a loss of power now over to the Configuration_adv.h search for POWER_LOSS

then uncomment the above this is set up for my printer mainboard so pin number might need changing on your device. and purge and retract might need changing as well.

will compile this after making other changes for the filament runout sensor

Filament runout sensor big tree tech

As I waiting for this to arrive seller sending another one middle of February so instead of moping around the workshop getting ready for it all to arrive.

Ok have found a bracket on Thingiverse I am going to remix it so I can mount the bracket directly to my 2020 so will be adding 2 tabs in Fusion 360 so I make this a reality. first, I am going to import the mesh in and will draw two rectangles using the top face of the bracket I then extruded them by 4.40mm then made a centerline in a sketch and added matching holes time to print

Quick and dirty modification but will work.

I will print it shortly the spikes will print not sure why they ended up there are joys of modifying a mesh

Just waiting on the current print to finish should relay run the farm but need to get neon orange up and running it’s on my list of things to do. it’s a long list as always.

Printed ready to fit when I get the parts. just test fitted will just what I wanted.

works on 2020 fine.

As I now have the parts time to fit it all to the frame for real as the sensor has arrived.

hidden all the wiring in the frame with some clips.

Going to connect it to the mainboard E0-STOP port you will have to switch it on in the firmware pin 15 was already selected for filament runout.

Now you will need to turn it on in firmware so in configutation.h

find the following FILAMENT_RUNOUT_SENSOR and uncomment it like below.

Next, scroll down and uncomment the following FILAMENT_MOTION_SENSOR and FILAMENT_RUNOUT_DISTNCE_MM set it to 7

and with that just need to reflash with v5 of the mancave monster firmware on the mainboard and we should be good to go.

My Current Firmware CR-10 BTT E3 mini 2.0 with BTT UPS, BTT Filament runout sensor, BL touch and Neo Pixel 18 pixels installed compiled here if you want the vs code files ask and will happily link it for you.

all components are now installed going to join the 2 printer halves and running initial tests. fingers crossed before I permanently bolt them together. Wiring issue, not a big one negative on neo pixel is the wrong way around not a biggie just taken a photo of the pins.

Mine was the wrong way around so out with crimp tools and time to make it right.

remade the connection so let’s test it again. now seems to all be working.

Homes check bl touch works check hot end heats not working for heat bed erm ok not heating need to check the wiring.

Got a feeling negative is what I meant to pass through the SSR going to go back through my notes.

Was 2 issues had heat bed plugged into the extruder and hot end in the bed and the negative was positive no damage all fires up now and works

Just print the front left panel with a modified hole for screen cables. so going to leave that running overnight, just fitted and perfect so that’s finalised.

One thing i will need to revisit is the relay board but I think that will be done in the future as projects are already way overrun and used lots of PETG I really need to invest in centre callipers they are uber expensive one day shall order some.

Time to modifiy my racking

The next job is lowering the racking so I can fit the new printer on the shelf need to move the spool holders down and then drop the shelf level down by 15 cm approx.

cleared the shelf and now to focus on removing shelf and old wiring as will rehouse the wall-mounted pi down also binning cheep fans as they temperature should never get that great and the nose one of them I producing is bad.

Have managed to drop shelf approx 120 mm have refitted shelf and refitted Prusa’s have moved my pi off the wall and disconnected fan. I shall monitor CPU temp via the plugin.

space is ready for the new printer

Now to place the printer in its place well nearly first flash the firmware and cave monster ready for action well nearly as I want to finish off the mods before I set it in place.

TFT Screen firmware configuration

One final tweak I wanna look at is the firmware for the screen as want to disable a few features and rename some descriptions if I can not sure it’s possible. but by the power of google.

first up looking at the config.ini

In order for the TFT, firmware is able to provide all of its functionalities/features, ensure that the following options are enabled in Marlin firmware.

General options:

  • EEPROM_SETTINGS (in Configuration.h)
  • BABYSTEPPING (in Configuration_adv.h)
  • AUTO_REPORT_TEMPERATURES (in Configuration_adv.h)
  • AUTO_REPORT_POSITION (in Configuration_adv.h)
  • M115_GEOMETRY_REPORT (in Configuration_adv.h)
  • M114_DETAIL (in Configuration_adv.h)
  • REPORT_FAN_CHANGE (in Configuration_adv.h)

Options to support printing from onboard SD:

  • SDSUPPORT (in Configuration.h)
  • LONG_FILENAME_HOST_SUPPORT (in Configuration_adv.h)
  • AUTO_REPORT_SD_STATUS (in Configuration_adv.h)
  • SDCARD_CONNECTION ONBOARD (in Configuration_adv.h)

Options to support dialogue with host:

  • EMERGENCY_PARSER (in Configuration_adv.h)
  • SERIAL_FLOAT_PRECISION 4 (in Configuration_adv.h)
  • HOST_ACTION_COMMANDS (in Configuration_adv.h)
  • HOST_PROMPT_SUPPORT (in Configuration_adv.h)

Options to support M600 with host & (Un)Load menu:

Options to support dialogue with the host (as a prerequisite)

  • NOZZLE_PARK_FEATURE (in Configuration.h)
  • ADVANCED_PAUSE_FEATURE (in Configuration_adv.h)
  • PARK_HEAD_ON_PAUSE (in Configuration_adv.h)
  • FILAMENT_LOAD_UNLOAD_GCODES (in Configuration_adv.h)

Options to fully support the Bed Leveling menu:

  • Z_MIN_PROBE_REPEATABILITY_TEST (in Configuration.h)
  • G26_MESH_VALIDATION (in Configuration.h)

I didn’t use this as couldn’t get to compile I will revisit this

  • Z_STEPPER_AUTO_ALIGN (in Configuration_adv.h)

so that’s the merlin firmware now done not to look at the config.ini.

custom logo

cave monster

so lots of settings and functions here have changed a handful of colours and the way it talks to octoprint.

next up going to look at the actual firmware pre-compiled so I can see what changes can be made. that will be a separate blog post I have added a new icon set and flashed the screen with new firmware to see if it helps.

Dragon Hotend and issue correction

K decided I would go the full whole hog and upgrade the hot end as well. as I wanna look at the movement in the x carriage on the extruder bracket. I also why it is quite tight on the belt.

Issue 1

I fixed it was the hole the direct-drive bracket is bigger than the m5 to linear rail bolt hole so have used 2 countersunk screws to centre the bracket. works well,

Fitted the dragon

I have removed the old OEM hot end. 2 screws and that’s gone now to fit the dragon hot end using Capricorn petg tube between it and the direct drive all fitted now to put the hot end back together upgrade is done. but not quite right cannot get filament into hot end tubes not quite long enough so time to order a length of it so I can get this right.

Issue 2

I noticed there is a lot of friction on the belt so I am going to swap the pully end around as I want this to be smooth and can align the pully across the beam. 4 front screws removed. pully off and rotated now to put the machine back together much smoother think I have fixed it might need a slight tweak but let home the machine and see what happens.

just going to make a benchy test. before I fit the new flexplate.

running into issues with filament sensor the hot end now clogged got a feeling the Capricorn tubes melted so I am going to strip down the hot end tonight and have a look and see if it’s down to that as removed nozzle and still cannot get the filament to come through. have ordered a back up hot end the big tree tech v6 hot end and a fixing bracket as a backup as got a feeling this isn’t right.

will disable the runout sensor for the calibration as I have a feeling it’s thinking it’s a clog on the hot end even though there is now a clog.

removed hot and cleaned and the issue blockage in the tube put it back together loaded it ran 20mm through it and bam blocked again so might be my filaments shit or the tolerances of the tube is too tight might try a different batch and see if I get any joy other wire going to revert back to my back up but that’s going to delay first print. by 3 weeks but going to launch this part of the build and then come back when it’s all printing right. at least makes me know that the runout sensor working. so will re-enable it after I have a calibrated machine.

going to first install the flex plate whilst i figure this out.

BISQU Flexplate

This is something I love on my Prusa printers will hopefully be the same experience. so to install going to need to stick the magnetic sticker to the glass bed.

so have turned over the glass sheet and cleaned it using isopropyl now to apply the sticker sheet went down will not be 100% straight but no one will notice.

before I test the plate on top. going start by resetting the EEPROM and then going through calibration again as don’t want to mess the sheet up. but that will be in part 7

all fitted now a waiting game for the new hot end so will leave this here final part will be testing it all out.

CR-10 Upgrades part 5

A happy New year to you all, Incoming parts have arrived so time to finish off this project last 6 upgrades firmware recompile and hopefully will be all done.

  • Y-Axis Linear rail upgrade
  • Neopixel install

Y-Axis Linear rail upgrade

You can get the kit I used here.

Yay The kit arrived when I was away so a bag of bolts and t-nuts aluminium end plates and base plates.

this is going to evolve some guesswork as with all china kits they never provide any instructions but basically will fit the 2 cross braces and add the rails to both and bolt them down will leave the supports lose so I can make sure all is plumb and attached the bed this is in theory fingers crossed.

Wow, they are tight going to loosen the frame ok now to centre them as best as I can. Now that I have the 2 cross members installed loosely to add the linear rails and 18 nuts and bolts on each rail to bolt them down lining them on the cross brace.

Now to mount the bed to the rails start with one side front bottom placing aluminium spacer and 30mm bot I fix in place I can see the left is off so nudge them to line up so I can put a bolt now to install the remaining 14 spacers and nuts. bed or carriage is attached I check it for lateral movement nice and smooth so I reattach the belts and repeat can that the top needs to come over. now I have it centred time to tighten everything up oh then looked at reference images of add noticed as i had 3 bits left that i couldn’t identify.

They are to make contact with the end stop. so add them now to install the rail end plates so another 8 screws and t-nuts. 4 aluminium covers later it’s done

Now waiting on spacers for the bed as I manage to lose once so should have them Friday also chatting with the vendor as my big tree tech package has gone missing in my absence. below is a montage of what happened through the build.

Neopixel install

Bit of 3d printing have found a led tape mount that I have modified to fit the gantry perfectly I am currently printing the bars in 2 parts will then print the end caps. 3 hrs later will just do a test fit tonight. ok, the first attempt failed so going to print into parts and have gone for a solid infill to reduce the movements see how it turns out. the bit that did print fitted though.

failed again argh going to look at slowing the print down to see if I can get it to complete

attempt number 3 with a raft this time let’s see if these thin columns will print.

So added a raft fingers crossed. Update 50% done still holding.

I miss calculated the length going to use a failure so sort it so chopping down a failure bit. also need to get a heat gun on it to take away the stringing.

made a mall 30mm section out failed parts and put 12v thought it to see if it lights and it did now to finish the cable.

lights up now to finish the cable.

right, this is going to be a bit of guesswork I will need to see how it pans out as I have changed my mind on how I am going to set it up but from what I can see I will need a 1000u competitor and 330k ohm resistor the competitor will go between ground and live and the resistor will go in line with data wire. I will make a 3 pin JST Xh connector so I can plug it into the mainboard this is the simple part. to install it I am going to stick the 18 LEDs to the top bar of the printer and stick it the v slot or I might stick it to some insert clips I have found that will allow me to stick it to it. still toying with this as I type this post. now the firmware is where I am going to start asking more questions as no one seems to be able to answer my questions. argh, have contacted support as they all seem to be for an earlier version of marlin firmware see what they come back with.

Figured I all out myself and was it a fucker so bugfix changes layout you will need to go ini folder in vs code fetures.ini and then change the following. go to adafruit comment on neopixle_led change to the following. NEOPIXEL_LED                           = https://github.com/CommandoreBombardiero/Adafruit_NeoPixel as shown below.

Now go configuration.h and search NEOPIXEL then change like below.

corrected code

Then build it will fail with something about the delay so then go find Adafuit_neopixle@src- some numbers and letters you will need to change the location in the brackets to the location of your delay.h file in marlin/hal/shared/delay.h can see it for my dropbox location below.

build it again might fail but then if you build one more time success, wow my mind is numb now only taken the best part of 3 weeks on and off to get this to compile now to make and add connectors and hopefully, it works.

Next, up now I have it compiling is to make up a 3 pin plug so looking at pinout i know i will need a 3 pin JST connector and 3 crimps and JST crimping tool this is fiddly could also be done with Dupont connectors if you didn’t have JST ones kicking around.

Time to update the firmware wish me luck. sd card in hand. a bit nervous lol.

hmm, not working I am not sure if it’s the wire or something else going to check through my notes and see if it’s something like the wrong controller pin or it’s tested the wiring and got a continuity check on negative and positive.

checked over the firmware code and had assigned the driver pin as 4 instead of PA8 will flash the firmware again v4 I change the version number each time I make changes to the code.

Now to put every thing back together and add some cable managment an figure out a way to mount the unit to botom of the printer well untill i figure out my next mod more on that in part 6. will also need to re calibrate the first layer again hoping for the last time.

Once dialed in going to start running parts for the next modifcation going to take a few weeks to get bits in from china and ooznest also got to rework some bits as well. going to do the rework first before spending out on parts. as all these mods hav spireled out of control.

Next steps

When the bits turn up from china I need to enable filament runout sensor and power loss in the firmware but that’s a lot more strait forward.

Will make changes to config.ini for the screen when get the new bits as will allow the main board and Octoprint to communicate with filament runout sensor as that’s where its plugged in.

We’ll all short lived control box don’t fit under machine to going to make something better see part 6

CR-10 Upgrades part 4

So this is all going to be 3d printed mods I have already done a 35hr print on the control board side I have printed the new feet need to print the SSR module clip might set that up whilst I am remote in wales the joys of being connected. so all I will need to do is 2 lids then will be ready for the pro upgrade.

also mounting on the screen on the side of the machine. might need to reprint the printing bracket. as want it on the left-hand side of the machine.

23hrs of printing done should be finished by the end of the day,

so just uploaded it to the local computer and now have kicked off the amazingly long 23min print haha so will only be 2 x 7hr prints left when I get home on Monday. just as I feared the small print it failed never mind noticed and cancelled the print. will check back with the main print later.

80hrs combined printing still a little cleaning to be done

wow, that’s the long prints done now for some smaller prints and armed with elnet the king of hair spray when it comes to getting prints to stick well. as Pritt stick is too messy. wow just saw the bend in the heat bed how did that happen bent it flat again. just going to adust the bed by probe till it’s nearly on the money then I might lock tight them in position for the moment. probably should have done that before I kicked off an 8hr print.

5 layers of 95 done

I will be going over to a flexible steel bed soon but till then I am going to continue on the old fashion way well till the credit card bill rolls and I then have my monthly spending pot.

lids and SSR printed and that just under 1kg of filament was done. on the case.

so time to strip out the old box and fit the electronics in the new one oh and to add the new feet so it will fit.

just need to order some silent fans as the control box fan is really annoyingly loud so I have orderd 120mm nocturia fan and I think i will need to order 80mm one for the PSU supply. I will be opening that up in the rebuild as one i dont know its voltage and 2 pin numbers 2 or 3 so will order that when i konw.. I then have to think about speed control as i don’t think they need 100% speed but that I will be looking into as we go, as going to monitor temprature with a probe in the electronics low voltage box.

Have been thinking about a name for my cr-10 modified machine that came up with cave monster. so the next round of modifications to the code will include a name change haha. will attempt to design him a logo as well for the boot screen.

as i have been spending alot of time getting everything printed for the next step i have been customising my octoprint layout and feel. also on christmas crafting for friends and family so yes been a fun week that and i am re jigging the work shop as need to add storage for extra tools as need to make it all work.

High voltage side.

time to look at power supply and lable up wring before i strip it out the box. next up power input and switch. I will be making new wiring for all power elements. First up adding the mains power plug and switch. looks like the are going to need a little help fitting so out with the dremal and they now fit. as it cold have stopped halfway through the job as working how and where to route the wiring and fit the ssr to the psu.

Also, going to wire the printer PSU through a 5v relay so i can turn the printer on and off through the raspberry pi cover this in the Low voltage side of the board but will cover that later.

Low voltatge side.

Now i have the power run across the board I will either add the bucks converter to step the 12v down to 5v to run the raspberry pi or I will use a mains adapter this will allow me to shut down the printer where as the other way would be a total power off. whilst I think I will install the pi and the main control board. am then going to install 2-way relay board so i can switch on/off the machine and lights via the relay.

Time to connect all the power wires and the heater wiring to the board and the SSR.

Now to add all the board inputs and output so end stops motors and sensor

next, it is time to fit the 120mm fan to keep things cool as its a 4 pin I will only use the 12v supply as should work will test this theory later also waiting on t-nuts so I can bolt this to the frame should have them later on today so will finish wiring ready to bolt it all together.

got one more print to go on as adding halo light to the camera so I can film all the loverly creations that I am making with the printer but that will be done once I have installed the rest of the electronics. going to make the camera mount a little more sensible as i feared there’s a little bit of a wobble when running.

testing halo /focus mount is not 100% right but fits and works soldered some longer wiring i will be

As I am waiting on parts as amazon let me down I will be getting the last bits sorted ready to bolt the boxes to the bottom of the printer. ok been a week had a family issue that’s now come to a sad conclusion. so back in London will try wrapping this stage up by Xmas but see what happens.

How my plans have changed

its been 2 weeks of hell over Xmas father in law passed away suddenly so was in wales for a week then came back to london and wife and son both have covid so stuck in london in the house i am negtive and they are both ok.

bad new but good news been working on the project and ironing out my kinks with it so where to start

It dont fit under my printer bed like its ment to due to my custom bed so instead of having a hissy fit throw 70 hrs printing. I am going to let be and will figure it out as i go i have welded the 2 sides together with some high strength glue and exsellitator now bonded together

i then have added some custom stand offs for the fan speed controler and 2 channel relay. i then drilled holes for external raspberry pi power and for fan controler knob. oh and power connector for the halo.

bit of wiring changes to the printer can be powerd off and on by the raspberry pi also using the 12v psu to power the halo light as well also had to change the wiring.

and we are good to go i am waiting on the next mods to show up from the far east got one PCB board still to fit so before i bolt it back together and start testing the new fetures

ready for install just power headers for the pi and add USB PCB when it gets here.

I will leave this here. get ready to part 5 this will be the final part i hope. so whats coming well a UPS 12v board from big tree tech. New fexable bed for the machine and fliminet runout sensor from big tree tech and upgraded linier rail upgrade and thats it.

i think after that i have run out of mods.

see you all in part 5.

CR-10 Upgrades part 3

Well as I await parts I will be working on a few issues and also designing some parts.

What I did not mention in the last part is I managed to drop the control box moving the printer back into the cave as it’s so big and the doorway is so tight. it is back in the cave no so I need to do a strip down and see what’s making my Y-axis go in reverse.

I have a feeling it’s damaged cable or end stop both are on order so should start on this shortly as really thought I had come to the end of the update journey. But no it’s become a paperweight well hopefully not for much longer.

So in part 3 plan is as follow.

  • Fix reversed Y-Axis after drop
  • Time to invstigate whilst i wait for new bracket
  • Fit proper X-axis linear rail bracket.
  • Reinstall hotend with direct drive & Install new hotend part cooler mod
  • Print a camera mount:

Fixing the reversed Y-axis:

this was working right till the control box that was balancing on the bed fell off and dangled. now the printer when homing goes in reverse. very odd I have ordered a new wiring loom and end switch. going to start by swapping the bent up end stop. that main pull was on and replace y loom fingers crossed. The end stop has arrived going to fit it now and see if that fixes the issues. If not back to waiting for the loom.

Looms arrived was the Y-Axis end stop wiring has broken out with the old in with the new.

Installing the updated motor mount and bed upgrade:

After ruling that wouldn’t fit the mods and I didn’t think they would fit.

I changed my mind and thought what’s the worst that could happen? So have fitted both the bed wasn’t too bad once I had lined up the centrical nuts up. I then added the new motor mount this wasn’t as much fun, as mounting it needed some parts that were not included. fist up need M5 T-Nuts luckily I had some, countersunk m5 screws again luckily I had these. right now to reattach the Y-Belt to the motor and the bed. for F#&k sake the belt is 100mm too short. looked through my draw of printer parts and spotted gt2 belts was a loop cut i and then rethreaded the bed. ok no to reattaching the end stop it wouldn’t fit as the holes in the bracket are for the raw small micro switch so have mounted the original end stop back in place if this causes issues can modify the end stop to fit on the brackets with old bent up microswitch scavenged for bits let us see hopefully not but have a backup plan.

all back together and homes ok so now for the next part of the project.

Time to invstigate whilst i wait for new bracket:

Now that I have a working printer going to do some more testing to see why it’s not printing right.

ski jump did hit camera mount im testing for later. bars hav foiled my install idea.

right has put a spirit level and my z was out slightly so have adjusted one of the rods. and the new result is better but still off. Hoping on the bracket to sort this out a bit better.

Just waiting on the arrival of the X-Axis bracket now as I am sure there that that is also compounding this. So as you might have figured I am doing other bits whilst I wait and updating this post as I go. Hoping by the end this will be an awesome printer.

The bracket is in the UK just waiting on delivery so probably in 48hrs time. so time to strip off The offending bracket and strip down the hot end ready for the new bracket to arrive

Fit proper X-axis linear rail bracket.

Out with the v2 bracket as there’s a 5mm difference between the centres. as you can see I have removed the modified direct drive hot end as I think this is also the issue with print being fine on one side and in the bed on the other. time to add the bracket and fit the 2 screws. before moving on to the hot end and direct drive. it fits but!! mgn9 rails kit not 12 argh never mind ordered new rail so will sort this out next week.